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OzECruisers General Discussions E/N/D vehicles General Discussion ONLY. NO TECH THREADS |
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12-06-2005, 04:24 PM | #1 | ||
Hmmm Gold!!!
Join Date: Dec 2004
Location: Brisbane, Northside
Posts: 331
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First if all, YAY!! : its all going. After a few mishaps it all going sweetly.
The first mishap was moving the damn aircon tensionor pully, eventually got that moving, felt quite stupid after realising how to do it.... then out came the old manifold, didnt take as long as i thought it would actually, that left me with a very empy engine bay, as quite excited. next all the plumbing was changed over, nothign real exciting there to report. then in with the new manifold, pluged it all in ( or so i thought ), bolted it all up, waiting for teh big moment, and nothing, just some clicking... not cool we dicovered a red wire that we had no idea what it did, straight on the forums i went, figured it was the starter motor relay, manifold off again... plugged it in, manifold back on and hey presto, it cranked, but that was it.... next we went thru the list of what it could be, it cranked, there was spark, next was fuel, none, took off the outlet hose, none in the rail, took off the inlet, there was plenty in there, most of it ended up in my eye : after getting the regulator off and looking at it like i knew what i was doing...i had a look thru the manual and discovered that i had the hoses on the wrong way.... : swapped them over, primed the rail, cranked it it it worked!!!!! : had a play around with the idle as it wasnt real flash. did a bit a dance and jumped around a bit like a fool, hey, i was happy! new accelerater cable in, checked everything was in order and took her for a fang around the bolck, :eclipsee_ felt it instantly, heaps more power, theres now a few more black lines around my area. over all, im VERY happy with the conversion if anyones interested i now have a fully functional cfi manifold for sale plus all bits needed for a mpi to cfi refit thnks for replying to my dumb posts about how to undo stuff theres a couple of pic just to prove that it went in bender
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1990 EA Series 2 Fairmont, Low Springs and shocks, 17 x 7 Advanti Flash Mags running on Falken rubber :, EL XR8 Sway Bars, NGK Iridium Plugs, New Trip Comp, Pacemaker 4480, 2.5 system 4L ED engine with surecam Now Sporting - OED666's 202+ RWHP engine!! :dj: fully
Last edited by EA_Bender; 12-06-2005 at 05:36 PM. |
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12-06-2005, 04:26 PM | #2 | ||
Hmmm Gold!!!
Join Date: Dec 2004
Location: Brisbane, Northside
Posts: 331
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well those pics suck, but u get the idea....
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1990 EA Series 2 Fairmont, Low Springs and shocks, 17 x 7 Advanti Flash Mags running on Falken rubber :, EL XR8 Sway Bars, NGK Iridium Plugs, New Trip Comp, Pacemaker 4480, 2.5 system 4L ED engine with surecam Now Sporting - OED666's 202+ RWHP engine!! :dj: fully
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12-06-2005, 05:06 PM | #3 | ||
Banned
Join Date: Dec 2004
Posts: 4,078
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ahhh another one down. Good shit, yeah those pics suck, but i get the idea. I bet the power comes on smoother too. Enjoy it, and congrats.
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12-06-2005, 05:33 PM | #4 | ||
Guest
Posts: n/a
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dam i must get around to doing mine as its really sucky and slow
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12-06-2005, 06:06 PM | #5 | ||
Last warning
Join Date: Dec 2004
Location: Mornington Peninsula, Victoria HeadCount: 3
Posts: 11,194
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that rocker cover looks awesome
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FALCN6 - Turbo, Air Bag Suspension - Hibernating EL GT - Supercharged NASCAR - 83 Thunderbird , Bagged DAILY - BA Fairlane Ghia, Boss 260 Turbo OFFROADER - Ford Explorer |
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12-06-2005, 07:12 PM | #6 | ||
Banned
Join Date: Dec 2004
Location: South East Melbourne
Posts: 6,156
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You took the manifold off to plug that wire in? Jeez...it's not that hard!
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12-06-2005, 07:20 PM | #7 | ||
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Join Date: Dec 2004
Location: At your U.B.
Posts: 2,099
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I had to lay under the car to plug that wire in. manifold off was a bit extreme. did you rewire the idle control circuit?
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EF Falcon Sedan 5.0 auto with IRS "the man that crashs AFF" |
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12-06-2005, 07:21 PM | #8 | ||
Custom user title
Join Date: Jan 2005
Posts: 1,892
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man... thats alot of work pulling the manifod of for a wire.. but at least ya good at it now :>
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12-06-2005, 07:30 PM | #9 | ||
FF.Com.Au Hardcore
Join Date: Jan 2005
Posts: 2,728
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im currently in the middle of a whole MPFI conversion in my 1989 EA....slapping a 4.0L EB/ED engine cant wait, i herd so many stories how MPFI is alot quicker....i h8 CFI , i just wanna try MPFI in it now !
-Grechie |
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12-06-2005, 08:53 PM | #10 | ||
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Join Date: Dec 2004
Location: At your U.B.
Posts: 2,099
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I garuntee that rocker cover will leak at the front and back t the half moon bits.
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EF Falcon Sedan 5.0 auto with IRS "the man that crashs AFF" |
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12-06-2005, 11:28 PM | #11 | ||||
Hmmm Gold!!!
Join Date: Dec 2004
Location: Brisbane, Northside
Posts: 331
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Quote:
Quote:
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1990 EA Series 2 Fairmont, Low Springs and shocks, 17 x 7 Advanti Flash Mags running on Falken rubber :, EL XR8 Sway Bars, NGK Iridium Plugs, New Trip Comp, Pacemaker 4480, 2.5 system 4L ED engine with surecam Now Sporting - OED666's 202+ RWHP engine!! :dj: fully
Last edited by EA_Bender; 12-06-2005 at 11:30 PM. Reason: spelling |
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13-06-2005, 12:06 AM | #12 | ||
Low and Loud
Join Date: Dec 2004
Location: Melbourne
Posts: 3,273
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Good to hear it all started to work out for ya ;)
burn the CFI manifold LOL like someone did :P while your at it burn my car :P LOL
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1993 Ford Fairlane NC3 Silver - LTD mockup, Worked V8 & Auto, Fully Optioned, Half of my Audio department at work installed in the car 1993 Ford Falcon XR6 Poly Green Stationwagon - 4.0 I6, Auto, 3:45LSD, All the usual XR6 Stuff but in a wagon : |
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